Today I finished cutting and drilling all the parts of the cart. I started with a new piece for the arm that connects the front section to the bearing shaft. The old one was pretty rough on one side since we cut it from an angled piece. Since I had to attach stuff to the top and bottom of the arm, I decided to cut a new arm from the pieces I bought from Online Metals, which gives me nice flush mounting on both sides. Drilled a bunch more holes with the drill press and discovered a few things:
- It is much easier to see the spot punched in the metal if you remove the paper template you used for punching.
- A small drill bit will usually “pop” into the punched spot, making things line up very nicely.
- A large drill bit has a mind of its own and tends to ignore the punched spots, giving me terrible hole alignment.
- Next time, for any hole about 1/4” or larger, I will drill a smaller hole first, then make it larger.
- When drilling a really large hole, start small and step up slowly. Large steps make the drill chatter.
After drilling several holes that didn’t quite line up, I had to fix them. My first effort is to just drill a slightly larger hole. If that doesn’t work, I use a rotary file to enlarge a hole in a selected direction, making it a little more like a slot.
The final cart assembly looks pretty good. I mounted all the different components onto the cart. I put the broken encoder in the position for the pendulum so I can test the pendulum without breaking another encoder. After I am comfortable with the pendulum behavior I will switch to the working encoder. I used a couple of cable ties to keep the wires from bending and breaking. Eventually they will be replaced with a cable carrier. Funny detail – every set of screws in the cart is a different size and type. It has metric (M3, M6), english (8-32, 10-32, 4-40), pan head, button head, flat head, slotted and phillips.
The next step is to attach the bearing shaft to the shelf at the right height so that the cart is horizontal and the pendulum will swing vertically. Getting the height right could be tricky. I also have to figure out how to make the pendulum so the hole is centered and straight. Then I will be all set for a control system. I hope that sbRIO board gets repaired soon.







